Comanche Peak Nuclear Power Plant
Comanche Peak Nuclear Power Plant is located in Somervell County, Texas. The nuclear power plant is located 40 miles (64 km) southwest of Ft. Worth and about 60 miles (97 km) southwest of Dallas. It relies on nearby Comanche Creek Reservoir for cooling water. The plant has about 1,300 employees and is operated by Luminant Generation, a subsidiary of Vistra Corp.
Comanche Peak Nuclear Power Plant | |
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Comanche Peak's twin containment domes in August 2017 | |
Country | United States |
Location | Somervell County, near Glen Rose, Texas |
Coordinates | 32°17′54″N 97°47′6″W |
Status | Operational |
Construction began | December 19, 1974 |
Commission date | Unit 1: August 13, 1990 Unit 2: August 3, 1993 |
Owner(s) | Luminant |
Operator(s) | Luminant Generation Company LLC |
Nuclear power station | |
Reactor type | PWR |
Reactor supplier | Westinghouse |
Cooling source | Squaw Creek Reservoir |
Thermal capacity | 2 × 3612 MWth |
Power generation | |
Units operational | 1 × 1218 MW 1 × 1207 MW |
Make and model | WH 4-loop (DRYAMB) |
Units planned | 2 × 1700 MW |
Nameplate capacity | 2425 MW |
Capacity factor | 95.1% (2018) 88.40% (lifetime) |
Annual net output | 19,356 GWh (2021) |
External links | |
Website | www |
Commons | Related media on Commons |
The Engineer of Record is Gibbs & Hill, Inc. of New York, New York.
Construction of the two Westinghouse pressurized water reactors began in 1974. Unit 1, originally rated at 1,084 MWe, came online on April 17, 1990. Its current, 40-year operating license is valid until February 8, 2030. Unit 2, 1,124 MWe, followed on April 6, 1993 and is licensed to operate until February 2, 2033 when it has to renew its license. As of 2023, Unit 2 was the fourth-to-last power reactor to come online in the United States, followed only by Units 1 and 2 at Watts Bar and Unit 3 at Vogtle.
In June 2008, the U.S. Nuclear Regulatory Commission (NRC) approved a request to increase the generating capacity of Units 1 and 2 by approximately 4.5% each. Luminant Generation Co. implemented the changes during refueling outages. Unit 1 was uprated in autumn 2008 with a capacity increase of approximately 1,210 to 1,259 MWe and Unit 2, the capacity of which rose from an estimated 1,208 to 1,245 MWe, was uprated in autumn 2009.